D7029
(Beyer
Peacock No. 7923)
| Delivered | 05/04/62 |
| To Traffic | 16/04/62 |
| 16/04/62 | 88A Cardiff Canton | Code changed to 86A from 09/09/63 |
| 08/65 | 82A
Bristol
Bath Road |
|
| 08/67 | 84A Laira | |
| 11/67 | 82A Bristol Bath Road | |
| 04/68 | 81A Old Oak Common | Code changed to OC from 06/05/73 |
| 15/01/75 | To store | Used as depot shunter until 03/02/75 |
| 03/02/75 | 81A Old Oak Common |
| From | To | Repair - Work carried out. |
| 26/07/62 | 09/08/62 | Heavy - Transmission change |
| 08/04/63 | 19/04/63 | Heavy - Engine change and modifications |
| 26/07/63 | 07/08/63 | Heavy - A and B bogie change and modifications |
| 16/04/64 | 01/05/64 | Unscheduled - A and B bogie change, boiler change and modifications |
| 20/05/65 | 25/05/65 | Unscheduled - A and B bogie change and modifications |
| 15/12/65 | 11/02/66 | Intermediate - Engine and transmission repairs, A and B bogie change, body repairs, modifications and experiment fitted. |
| 03/01/67 | 10/01/67 | Unscheduled - Body repairs |
| 08/01/69 | 10/01/69 | Classified - A and B bogie change, modifications and experiment fitted |
| 17/03/70 | 21/05/70 | Intermediate - Engine change, transmission change, A and B bogie change, modifications, collision damage to both cab ends. |
| 16/04/62 | 17/03/70 | Green - Standard Yellow Warning Panel |
| 21/05/70 | Withdrawal | Blue - Full Yellow Ends |
Withdrawn:
28/02/75
Mileage:
Not known
Last working :
20/02/75
6A27 11.55
Malago Vale - Old Oak Common.
D7029 was built as part of an order for 101 type '3' diesel hydraulic
locomotives. The order for the class was placed in June 1959 but it wasn't until
the 5th April 1962 that D7029 was delivered from Beyer Peacock to
Swindon Works. After weighing and acceptance trials in works D7029 was trialed
to Stoke Gifford on the 16th and handed over for service that
afternoon. Allocated new to Cardiff Canton D7029 settled down quickly to working
express trains from South Wales to London, amongst the more prestige jobs was
the Red Dragon which ran from Swansea to Paddington.
A brief spell
at Plymouth Laira from August to November 1967 saw workings into Cornwall but
within three months D7029 was transferred back to Bristol Bath Road. The move to
Old Oak Common took place in April 1968 and it was this depot that would be
responsible for looking after D7029 for the next seven years, until its demise
in 1975.
A collision
occurred in March 1970 involving D7029 where it was damaged at both ends. The B
end sustained buffer beam damage, forcing the buffers downwards and the A end
cab sustained a large crease in the cab front. Although no details are known
about the incident the evidence suggested D7029 was run into at the B end and
its train piled into its rear (A) cab, riding up over the buffers. The damage
sustained to the cab frame in one corner is still present on the locomotive,
Swindon patching up the damage suitably enough to return the locomotive to
service. It is our intention to remove Swindon's' repair and carry out the frame
repairs that Swindon should have done! When released from Swindon on the 21st
May 1970 D7029 sported a new coat of paint in the new corporate Blue livery.
Being an Old
Oak Common based locomotive saw it used mainly on the Paddington to Worcester
& Hereford route with frequent use on Oxford commuter services. Freight work
was confined to trip workings around Park Royal and Greenford as well as cross
London service from Acton to Willesden and Temple Mills.
The decline of
the class began in earnest from 1972 onwards when they lost the Bristol to
Portsmouth and Weymouth services to S.R. DEMU traction and the South Wales
services to DMU and class 37 traction. By January 1974 there were just ten
examples of the once strong 101 class left in service. Brush Type '2' class 31's
started to infiltrate services once the stronghold of Hymeks reducing them to
more and more freight workings, taking them to South Wales and Devon. As New
Years Day dawned in 1975 only six remained and D7028 would succumb that same
day.
Detailed
records of the mechanical history for D7029 have been saved by the group from
British Railways. The full history from the Swindon Works maintenance folder has
also been saved.
The beginning
of the end for D7029 had started on the 17th December 1974 when the
loco was stopped at 05.00 for reported fuel dilation. Engine repair work was
started by the night fitters from the 16th and continued with less
and less enthusiasm until, on the 19th, work stopped completely.
Pushed out of the factory to release space for other more important locomotives
D7029 was positioned outside the factory. The loco remained in this condition at
Old Oak Common until the day shift started at 08.00 on the 3rd
January 1975. They started to rebuild the engine and requested that the loco be
brought inside to be put on charge, a task not carried out until the 10th
when space became available. Eventually it was the afternoon shift on the 15th
that handed D7029 as fit for traffic, only to be told that the locomotive was to
be confined to shed and used as the yard pilot! This is how D7029 was destined
to remain until, on Sunday the 2nd February D7022 was failed, at
23.00, with engine stopping faults, that is to say it just kept shutting down.
The decision was made to return D7029 to traffic in its place. Given a
Ultrasonic Axle Test and a brake block change D7029 was trialed in the yard,
operated in 'power' and all safety systems checked. Once these were proved to
have operated correctly D7029 was returned to traffic as of 05.00 on the 4th.
Having spent
the majority of its new lease of life on trip freights from Acton to Park Royal
and Southall mixed in with Cross-London freights the final days in service for
D7029 was almost top link work!
On Saturday 15th
February D7029 worked 4B05 05.15 Paddington to Bristol parcels and came back on
4A39 empty vans at 14.00 from Malago Vale. Resting at Old Oak all day Sunday the
next duty was on the 17th performing a local Acton to Slough
engineers train.
Stopped at 01.00 on Tuesday 18th February at Old Oak Common for 'C' exam the loco was returned to service at 14.00 on the 19th, returned to service as spare. On the 20th Control used D7029 on another trip to Bristol, still with 4B05 but this time returning on 6A27 11.55 Malago Vale to Old Oak Common empty vans. Unfortunately D7029 was failed on the 21st at 05.30 with coolant water coming from tell-tale holes on No. 15 cylinder liner on the engine. Stopped pending materials which never arrived saw the locomotive condemned on the 28th.